SOLAS compliance poor – lifeboat release hook failure identified in TSB investigation report

Poor compliance with SOLAS in 'Northern Ranger' incident
Poor compliance with SOLAS in ‘Northern Ranger’ incident

The Transportation Safety Board of Canada (TSB) has published an incident report on a lifeboat release hook failure during a drill on the passenger ferry ‘Northern Ranger’ in October 2017, which led to minor injuries. The failure was linked to poor compliance with SOLAS and the operator’s safety manual.

On 11 October 2017, the starboard lifeboat of the passenger ferry Northern Ranger was undergoing operational testing at the dock in Nain, Newfoundland and Labrador, when its forward release hook failed.

While the crew members were lifting the lifeboat to the vessel’s embarkation deck, the forward release hook suddenly released and the Continue reading “SOLAS compliance poor – lifeboat release hook failure identified in TSB investigation report”

Pacific 1: Poor decision to remain at sea during continuous flooding cited as main cause of sinking

Pacific 1
Pacific 1

The NTSB has published its investigation report on the flooding and sinking of the commercial fishing vessel Pacific 1 while in the Bering Sea, Alaska in February 2019. The report identified the master’s decision to remain at sea with continuous flooding as key cause of the sinking.

About 0330 local time on 15 February 2019, Pacific 1 was engaged in cod fishing in the Bering Sea near Kashega Bay, Unalaska Island, Alaska, when the vessel began to take on water at the stern. The five crew members abandoned the vessel and were rescued by the nearby Good Samaritan vessel Kona Kai. There were no injuries, but there was an oil sheen. The vessel sank and was considered a total Continue reading “Pacific 1: Poor decision to remain at sea during continuous flooding cited as main cause of sinking”

Poor hull maintenance linked to flooding of towing vessel Tom Bussler says NTSB report

Poor hull maintenance linked to flooding of towing vessel
Poor hull maintenance linked to flooding of towing vessel

The National Transportation Safety Board (NTSB) has published an investigation report on the flooding and sinking of towing vessel ‘Tom Bussler’ on Tennessee River in January 2019. The incident stressed issues associated with poor hull maintenance and repair.

On January 7, 2019, about 2030 local time, the towing vessel Tom Bussler was transiting in light boat condition (no tow) upbound on the Tennessee River at mile 15 near Calvert City, Kentucky, when it began flooding and quickly sank in the channel. Both crew members aboard abandoned the Continue reading “Poor hull maintenance linked to flooding of towing vessel Tom Bussler says NTSB report”

MFV Suzanne II: MCIB publish report on the fire and loss

MFV Suzanne II
MFV Suzanne II

Ireland’s Marine Casualty Investigation Board (MCIB) has released its investigation report on the fire and loss of MFV Suzanne II, east of Arklow, in May 2019. While the exact source of the fire is unknown, the report highlights that the quick response of the crew and their knowledge on when to abandon ship was key to their successful rescue.

On 2 May 2019 the MFV Suzanne II, a fishing vessel, was stopped 30 nautical miles east of Arklow and the crew were taking a break between fishing activities when a crew member observed smoke coming from an engine room vent. The skipper went Continue reading “MFV Suzanne II: MCIB publish report on the fire and loss”

Red Falcon: Report on collision between ro-ro passenger ferry moored yacht at Cowes published

Red Falcon report
Red Falcon report

At 0811 on 21 October 2018, when navigating in severely reduced visibility in Cowes Harbour, the master of the ro-ro passenger ferry Red Falcon lost orientation when his vessel swung out of control, departed the navigable channel and was spun around through 220°. In his confusion the master drove the ferry in the wrong direction resulting in a collision with the moored yacht Greylag which was sunk on its mooring as a result.

Safety issues
the master became fixated upon the information displayed on his electronic chart Continue reading “Red Falcon: Report on collision between ro-ro passenger ferry moored yacht at Cowes published”

Lubrication oil filter was mounted poorly resulting in engine failure

Lubrication oil filter
Lubrication oil filter

Transport Malta’s MSIU has released an investigation report on the main engine failure of the oil/chemical tanker ‘MV Guroni’ while underway in January 2019. According to the report, the lubrication oil filter of the main engine had been improperly mounted, which eventually led to severe damages to the components of the main engine and a complete failure of the main engine.

On 08 January 2019, at 0742, while the vessel was navigating through Skagerrak, an oil mist detector alarm was observed in the engine-room, followed by a Continue reading “Lubrication oil filter was mounted poorly resulting in engine failure”

Yantian Express fire likely caused by coconut charcoal official report identifies

Yantian Express - Photo credit: Smit Nicobar
Yantian Express – Photo credit: Smit Nicobar

The Federal Bureau of Maritime Casualty Investigation (BSU) has published its investigation report about the causes of the fire in the area of the deck cargo on board the container ship Yantian Express, identifying coconut charcoal as the likely cause of the fire.

It was during the early morning hours of 3 January 2019 that fire broke out in the deck cargo in the area of cargo hold 2 on board the German flagged container ship Yantian Express. The ship was in the North Atlantic, due to reach Halifax, Canadathe following day. Continue reading “Yantian Express fire likely caused by coconut charcoal official report identifies”

MOB recovery equipment and drills inspections to be witnessed by MCA surveyors following MAIB report

MCA surveyors to witness inspections of MOB recovery equipment and drills
MCA surveyors to witness inspections of MOB recovery equipment and drills

The UK Marine Accident Investigation Branch (MAIB) has published its report on the investigation into an accident where a tug’s chief engineer lost his life boarding his vessel. The MCA has instructed its surveyors to witness inspections of MOB recovery equipment and drills following the MAIB report.

The accident highlights the forever-present dangers seafarers including tug crews face in carrying out everyday tasks and the difficulties reacting to incidents despite the presence of well-prepared procedures and equipment.

The tug was carrying out typical shiphandling and standby duties at a UK Continue reading “MOB recovery equipment and drills inspections to be witnessed by MCA surveyors following MAIB report”

MAIB makes urgent call for information on styrene monomer near misses or accidents

Fireball viewed from the Ulsan Bridge
Fireball viewed from the Ulsan Bridge

The UK Marine Accident Investigation Branch (MAIB) has released an interim report into the explosion and fire on board the chemical tanker Stolt Groenland, but before concluding its investigation, MAIB is calling for information regarding any accidents or near-misses involving the carriage of styrene monomer, including any actions subsequently taken.

The fire on Stolt Groenland occurred in Ulsan, South Korea, on September 28, 2019. The Cayman Islands registered vessel had sailed from Houston on August 17 carrying 20 different chemical cargoes in 37 of her 39 cargo tanks. At about 0600 on September 28, the Singapore registered chemical/product tanker Bow Dalian secured alongside Stolt Groenland’s port side. The purging of Bow Dalian’s cargo tanks Continue reading “MAIB makes urgent call for information on styrene monomer near misses or accidents”

Sugar beet pulp prone to ignition when moistured and heaped reveals investigation report

Image courtesy of www.shipspotting.com
Image courtesy of www.shipspotting.com

The Federal Bureau of Maritime Casualty issued an investigation report on vessel “Ventura”, to look for the causes that resulted to the vessel’s cargo tanks and cargo being burnt down, highlighting that sugar beep pulp is prone to ignition when moistured and heaped.

Specifically, the Antigua and Barbuda-flagged multipurpose vessel called “Ventura” began its journey from Liepaja in Latvia heading to Casablanca in Morocco on December 18, 2015.

The vessel was transmitting about 4,811 mt of sugar beet pulp with no added molasses. The vessel sailed by the Kiel lighthouse at 11.00, and at 12.00 smoke was noted onboard the vessel and triggering the fire alarm.

Continue reading “Sugar beet pulp prone to ignition when moistured and heaped reveals investigation report”

Combustible furnishings contributed to extent of fire on Grand Sun says accident brief

The National Transportation Safety Board (NTSB) has released a Marine Accident Brief about the fire on the offshore supply vessel Grand Sun, noting that substantial use of combustible wood paneling and drapery contributed to the extent of the fire.

The vessel was transiting the Chandeleur Sound in the Gulf of Mexico, about 15 miles from the Chandeleur Islands, Louisiana, on October 8, 2018, when she caught on fire. The four crewmembers aboard attempted to fight the fire but were unsuccessful. They remained on the stern of the vessel until they were rescued by the U.S. Coast Guard. The fire burned itself out, and the vessel was later towed to port. No pollution or injuries were reported. The vessel, valued at $1.6 million, was deemed a constructive total loss.

Continue reading “Combustible furnishings contributed to extent of fire on Grand Sun says accident brief”

Aaron & Melissa II: Clogged bilge system and poor weather led to sinking

Aaron & Melissa II
Aaron & Melissa II

The National Transportation Safety Board (NTSB) has released a Marine Accident Brief about flooding and sinking of the fishing vessel Aaron & Melissa II approximately 70 miles southeast of Portland, Maine, while transiting to fishing grounds during a storm with gale-force winds.

The Aaron & Melissa II sank about 0800 local time on November 14, 2018. All four crewmembers abandoned ship and entered an inflatable liferaft when attempts to dewater the vessel proved unsuccessful; they were later rescued by a U.S. Coast Guard helicopter. Petty Officer Michael Kelly, a rescue swimmer with the U.S. Coast Continue reading “Aaron & Melissa II: Clogged bilge system and poor weather led to sinking”

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