Error in maintenance led to diesel engine failure reveals NTSB report

Left: EMD 710 cylinder arrangement showing the affected area in red. Center: EMD 710 connecting rod arrangement. (Photo credit: Dynamark Engineering)
Left: EMD 710 cylinder arrangement showing the affected area in red. Center: EMD 710 connecting rod arrangement. (Photo credit: Dynamark Engineering)

An improperly tightened fastener led to a diesel engine failure on a Washington State Ferries passenger and car ferry near Bainbridge Island, Washington are the findings of a National Transportation Safety Board (NTSB) report.

Marine Investigation Report 22/06 details the NTSB’s investigation into the April 22, 2021, catastrophic failure of the no. 3 main engine aboard the Wenatchee during a sea trial in Puget Sound. The failure led to the ejection of components from the engine and resulted in a fire in the no. 2 engine room. No injuries or pollution were reported, while damages were estimated at nearly $3.8 million.

In November 2020, the Wenatchee, operated by Washington State Ferries (WSF), was taken out of service for maintenance. During the maintenance period, two of the four main diesel engines, numbers 2 and 3, were overhauled by factory-trained technicians. Following the completion of engine overhauls the vessel crew conducted engine tests. Alarms activated for the no. 3 main engine. Crew members found pieces of a cigarette lighter in the lube oil system. Technicians returned to inspect the engine and recover the pieces, advising WSF it was acceptable to run the engine.

On April 22, while the vessel was conducting a post-maintenance sea trial in Puget Sound, the no. 3 main engine experienced a connecting rod assembly failure and ejected components that breached the crankcase, resulting in the ignition of hot pressurized gases that were released in the engine room. The crew of the Wenatchee effectively contained the spread of the fire by stopping all fuel supply and ventilation to the engine room and isolating the space.

The NTSB determined the probable cause of the mechanical failure of the no. 3 main engine was a connecting rod assembly that came loose and separated from the crankshaft due to insufficient tightening (torqueing) of a lower basket bolt during the previous engine overhaul.

“When installing fasteners, personnel should use a calibrated torque wrench, follow the manufacturer’s recommended tightening guide and torque values, and verify that all required torque requirements have been completed,” the Wenatchee report said. “Undertorqueing a fastener may cause excess vibration or allow the fastener to come loose, while overtorqueing may lead to failure of the fastener or the machinery component being secured.”

Download the full report:NTSB Wenatchee ferry report

Read another NTSB Report here: NTSB report determines probable cause in Miss Dorothy vessel towing fire

 

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